project:Soarer
So thankfully the dyno guy allowed me to personally make some tweaks/checks/adjustments while trying to tune this mfer. i finally tapped my wide band into the aem unit. brought a filter for my iaac unit. did my best to adjust the idle screw on the throttle plate.
things were going well then hit a skid mark when the dwell started acting up.
Still no dice, then he fixed the dwell got it rev then disaster struck.
my rings went kaput. did a compression test and only 1 cylinder was healthy, one was 30psi and one was 60.
so that was my tune for the day, i finished out at 263whp on 9 psi. (i need a ebc controller for the aem).
so i got a few qts of oil from the guys and made my trek back to Missouri, defeated but not done, i vowed to come back.
im thinking the rings went because of poor crank case ventilation, i plugged the pcv valves and ran 10an lines to an oil catch can with no vacuam.
i was also told the filter on top of the can was way too small.
Now(currently) it huffs white smoke and some oil out that same filter.
Last edited by megamax; Jun 25, 2016 at 09:09 AM.
so here we are again, faced with a 2jzge, and once again not 1 but 2 of the bolts don't want to cooperate.
so i had to get smarter than the bolts and mutilate them from within the block. luckily they were right next to each other.
then finally finally, the block was freed!!
never disassembled an engine before. so this is new territory for me. but looks like the bearings were not shot to ****.
im just looking to do a stock rebuild with stock size rings and some better x-bearings.
This thrust washer bearing thing is the most biggest problem i forsee for me.
and that is all i have so far, waiting on the machine shop to get back to me. he is charging me $250.00
-hot tank
-clean pistons
-polish crank
-hone cylinders
-install piston rings
Celebrating Lexus & Toyota from Around the Globe
there was no oil in the pistons or on the spark plugs? ?
The head guy told me it was normal for if your rings to go if they are weak AFTER a head job.
Good Luck on your next block build .
I see your still at it. Sorry about your mishap man. Stay positive, as you have displayed, and it will be soon over. I remember when I first heard mine run after all I went through. I couldn't have done it with Cartmill's help.
.20 over cp's.
I also opted to get some eagle rods, after buying/flirting with the idea of using rods from cx racing(took them back because the rod bolt was way smaller.
now I had time, so within 3 weeks I took my soarer out of service, swapped head and all the parts on the 2j block, swapped to the r-154 tranny I've had sitting for years and violia!!!
so first order of business was stripping the 1jz, all the stuff came off and I have it for sale for $200.00
then I snagged me a nifty cart to haul off the stuff that needed to be power washed!
-BLOCK WAS DECKED/BORED TO .20 OVER
-HOT TANKED
-CRANK WAS POLISHED/BALANCED
-PISTON RINGS WERE FILED/INSTALLED
-RODS WERE BALANCED/WRIST PINS INSTALLED
TOTAL BILL $870-930 (HAVE TO LOOK AT RECEIPT)
not what I wanted to spend.
also picked up some break in oil







